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Thai Nguyen province’s Luu Xa Cement Plant was built and
became operational from August 1995 as part of a national program on producing
three million tonnes of shaft-kiln cement and was a member of a building
material company under the Vietnam Industrial Construction Corporation. The
plant embraced on the cleaner production program which was presided by the Component
in Cleaner Production in Industry (CPI) since 2007. With active support from
consultants, the plant could save VND390 million in 2007 alone.
Employing a locally designed production process initially,
the plant has continually applied latest science and technology achievements to
innovate production technology. It has succeeded in raising its total designed
capacity from 60,000 tonnes/year initially to more than 100,000 tonnes/year at
present, creating stable work for over 300 laborers with incomes averaging
VND2.3 million per month and bringing annual revenue of over VND60 billion.
From small measures
From the inception, the plant’s management got to know that
shaft-kiln production lines were big energy consumers with most of the
equipment designed and installed locally. Therefore, along with effectively
tapping existing production lines and investing in specialized equipment for
dust and smoke treatment the plant had launched a series of emulation movements
in search of effective production solutions.
Its efforts to conserve energy were duly rewarded.
Accordingly, energy consumption was reduced from 1,450-1,500Kcalo/kg of clinker
in 1996 to 1,20Kcalo/kg of clinker in 2000, similarly power consumption was
reduced from 125-130kW/tonne of cement products in 1996 to 105kW/tonne of steel
products by 2000.
Significantly, since taking energy efficiency approach, the
plant’s management adopted a number of solutions to help conserve energy in an
efficient manner. Accordingly, production team leaders were encouraged to join
courses on energy efficiency, efforts were made to survey, check and draw up
careful analyses of production indexes, and enact energy consumption limits
pertaining to some production stages.

In particular, the plant had replaced 14 screw conveyors
frequently confronting breakdowns and bearing high overhaul and operating
expenses with reasonably priced kinetic lines with stable performance.
Estimates showed that the plant could save 3kW through replacing each conveyor
screw and save VND8.5 million in overhaul expenses annually.
Besides, the solution to install large-capacity inverters to
Road fan 215kW engines which were used to ventilate clinker furnaces helped the
plant reduce 21.4 percent of power consumption for Rood fans.
The plant had also taken numerous other energy efficiency
measures such as raising transformer
voltage level from 6kW to 22kW, renovating clinker furnaces and giving bonuses
to best performers in energy conservation and production fields.
High efficiency
Initially the outcome resulted from energy efficiency
efforts at the plant was modest due to the insider poor knowledge about the
cause. As of 2007 the plant has invested intensively into innovating equipment
and finding viable solutions to raise business efficiency.
The management said that the plant had taken a total of 19
energy efficiency solutions at a cost of more than VND1.5 billion by late 2007.
Accordingly, efforts were made to replace broken washers, install inverters at
suitable places and dispersion capacitors in areas nearby engines with more
than 22kW in capacity or rationalize engine loading capacity. The plant could
save VND390 million right in 2007, the first year it embraced the energy
efficiency approach.
In 2008, the plant continued implementing energy efficiency
solutions, focusing on innovating the material drying system to ameliorate
drying quality and reduce level of dust and mud emitted to the environment.
With a monthly investment of over VND1.5 billion, the solution helped the plant
save 5,000cu.m of water, reduce the number of cleaners, utilize 150 tonnes of
wet mud and save around 50 tonnes of soil and 25 tonnes of coal that were
formerly discarded.
Also in 2008, the plant pumped capital into improving
tempering technology and procuring a state-of-the art dust/haze filter system
for clinker furnaces costing more than VND3.4 billion. Thereby, the plant had
succeeded in lowering the dust/haze concentration at clinker furnaces from
305mg/cu.m to 42mg/cu.m and coal consumption from 0.241 to 0.233kg/kg of
clinker. These solutions helped the plant save VND603.8 million through using
less coal, electricity, clay and water and bettering laborers’ working
environment.
In the period 2007-2008 the plant injected more than VND6.5
billion in energy efficiency and cleaner production efforts which helped it
save over VND1 billion annually in the production cost, avoid emitting 178.5
tonnes of dust and 1,509 tonnes of dioxide carbon to the environment and
recycle 825 tonnes of waste materials.
The plant is embarking on an in-depth investment project to
heighten clinker production capacity and quality at a cost of around VND20
billion. Once completed, the project would reduce 15 percent of coal
consumption in tempering clinker and raise clinker quality.
Not satisfying with these attainments, from 2009 the plant
continued employing environmentally friendly techniques through cleaner
production and energy efficiency approaches. Significantly, in the coming
period the plant attempts to use low-quality coal for production to save cost,
in the meantime further invest in cutting-edge equipment to achieve both
production and energy expense targets, said the plant representative, Nguyen
Khac Duc.
By Tran Linh
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